MD11, Dublin Ireland, 2002

MD11, Dublin Ireland, 2002

Summary

On 3 February 2002, a Delta Airlines MD-11 encountered a sudden exceptional wind gust (43 kts) during the landing roll at Dublin, Ireland. The pilot was unable to maintain the directional control of the aircraft and a runway excursion to the side subsequently occurred.

Event Details
When
03/02/2002
Event Type
RE, WX
Day/Night
Day
Flight Conditions
On Ground - Normal Visibility
Flight Details
Operator
Type of Flight
Public Transport (Passenger)
Intended Destination
Take-off Commenced
Yes
Flight Airborne
Yes
Flight Completed
No
Phase of Flight
Landing
Location
Location - Airport
Airport
General
Tag(s)
Extra flight crew (no training)
RE
Tag(s)
Overrun on Landing, Directional Control, Significant Crosswind Component, Off side of Runway
WX
Tag(s)
Strong Surface Winds
Outcome
Damage or injury
Yes
Aircraft damage
Minor
Non-aircraft damage
Yes
Non-occupant Casualties
No
Occupant Injuries
None
Occupant Fatalities
None
Off Airport Landing
No
Ditching
No
Causal Factor Group(s)
Group(s)
Aircraft Operation
Safety Recommendation(s)
Group(s)
Airport Management
Investigation Type
Type
Independent

Description

On 3rd February 2002, a Delta Airlines MD-11 encountered a sudden exceptional wind gust (43 kts) during the landing roll at Dublin, Ireland. The pilot was unable to maintain the directional control of the aircraft and a runway excursion to the side subsequently occurred.

Synopsis

This is the synopsis from the official report into the incident published by the Irish Air Accident Investigation Unit:

"During its landing rollout on RWY 28 at EIDW, the MD 11, registered N803DE (Delta 129) started to initially drift towards the right and then slowly to the left-hand side of the runway. Efforts by the Captain, the pilot-flying (PF), to counteract this drift through the application of full right rudder and right tiller failed, and the aircraft departed the paved surface into the prepared graded ground, which was rain soaked. The Captain chose not to evacuate the passengers and crew through the emergency escape slides, preferring instead to wait for outside assistance and disembarkation by mobile stairs. After approximately two hours, passengers and crew commenced disembarkation through the forward right-side (R2) cabin door and down the mobile stairs where they were immediately bussed to the terminal building. There were no reported injuries."

The Report states the cause of the accident to have been:

"The cause of the runway excursion was that the aircraft was subjected to an unexpected and sudden wind gust during the initial stages of the landing rollout, inducing a rate of yaw to the left, which could not be controlled by the pilot flying."

Related Articles

Further Reading

SKYbrary Partners:

Safety knowledge contributed by: