Aircraft Load and Trim

Aircraft Load and Trim

Description

It is a legal requirement and crucial to the safety and structural integrity of an aircraft that it is loaded in such a way that the specified maximum allowable weights are not exceeded and that the centre of gravity as loaded will be within the permitted flight envelope and remain so for the entirety of the intended operation. Once these conditions have been satisfied, it is equally crucial that the flight crew are aware of the prevailing weight and centre of gravity so that they can set aircraft equipments appropriately; these include take off reference speeds, slat/flap position, and pitch trim or stabiliser position. This is important to ensure that the aircraft will achieve published certified performance and that the aircraft retains expected stability and control characteristics. It is also very important that aircraft baggage and freight load complies with the restrictions on carriage of dangerous goods.

Loading Procedures

It is essential that the Dispatcher, or other official assigned responsibility for overseeing aircraft loading, specifies the loading requirement correctly and has a reliable method by which he/she can be satisfied that his/her instructions have been carried out as requested. Whilst modern automated systems may determine the seating options for passengers and the load disposition, effective procedures and compliance remain the only way of ensuring that what has been specified and passed to the aircraft commander has actually been achieved. Specification of the hold compartment loading is usually achieved by the completion of a Loading Instruction Form (LIF). The LIF is given to the loading supervisor who certifies that it has been complied with and returns it to the issuer as evidence that the work has been completed. The completed load and trim sheet are then given to the aircraft commander. The human supervisor must also have a reliable means of confirming that if dangerous goods are loaded the dangerous goods regulations are complied with and a Notification to Captain (NOTOC) is issued and duly signed by the aircraft commander. The original NOTOC is retained by the aircraft commander onboard and a copy is held at the departure point. The human supervisor must also confirm that any special requirements for securing unusual items in the holds or in the passenger cabin have been complied with.

Fuel Loading and Distribution

Many swept wing jet transport aircraft use fuel distribution to optimize the centre of gravity in cruise to reduce fuel burn. This is achieved by keeping the C of G towards the aft limits of the envelope by utilizing outboard wing, aft body or horizontal stabilizer fuel tanks. It is the aircraft commander’s responsibility to ensure that the fuel load prior to takeoff is correctly distributed and reflected on the load/trim sheet and maintained within the prescribed limits for the remainder of the flight.

Load and Trim Sheets

The traditional method for ensuring load and trim compliance dates from the days when all load and trim sheets were completed manually on specific forms designed for use with each aircraft type, and is as follows:

  • the completed document is presented to the aircraft commander
  • the aircraft commander checks that it is internally consistent by carrying out some simple cross checks of input and calculated output data for gross errors and,
  • if the cross checks are satisfactory, the commander formally accepts the load and trim sheet by means of a signature on at least two copies, one being retained by the departure agent and the other by the flight crew.

The DCS (Departure Control Systems) process is slightly different in that only the input data need be checked and the completed document may not necessarily be signed by the agent presenting it, as he/she may have had no part in its preparation.

However, in both cases, the acceptance of an apparently correct load and trim sheet does not guarantee that the aircraft has necessarily been loaded as stated.

Example of a load sheet - in this case, the aircraft is a Citation X

Departure Control Systems (DCS)

Most Load and Trim Sheets used today in commercial air transport operations by multi-crew aircraft are produced by contracted Handling Agents who input flight-specific data into a proprietary DCS. There are a number of commercial DCS products available. Some are operated by large airlines for their own use and then also employed to generate external user business. Other similar DCS are operated independently of any particular airline. Where DCS are used, the data input and electronic generation of the load and trim sheet may be carried out at a regional centre and merely printed off, together with corresponding LIF, by the aircraft operator or the contracted handling agent employees. Note that DCS will only produce output data as accurate as the inputs, so it is important to guard against input errors.

Manual Load Sheets

Manual Load sheets involve a pro forma calculation of Maximum Ramp Weight (MRW), Maximum Take Off Weight (MTOW) and Maximum Landing Weight (MLW) whilst the centre of gravity is located by marking the requisite aircraft operating weight (vertical scale) on a ‘drop line’ located on a centre of gravity ‘index’ scale which forms the horizontal axis. If the position so found is within the areas shown as the permitted safe flight envelope, (and remains within the safe area as fuel reduces to planned landing weight) then operation as loaded is possible. Manual preparation of load and trim sheets used to be commonplace but they are now used so infrequently that recalling the necessary method can be challenging to ground staff and flight crew alike. Many younger pilots have seldom or never prepared a manual load and trim sheet or checked one for acceptance; this unfamiliarity significantly increases the risk of undetected errors with significant consequences. It is good practice to complete a manual load sheet once a month to develop and sustain proficiency against the day one suddenly becomes essential at short notice.

Aircraft Commanders' Acceptance of Load and Trim Sheets

The aircraft commander must be given a copy of the completed load and trim sheet for the flight and should check and sign it, leaving a copy at the point of departure. The aircraft commander is obliged to accept that the aircraft is loaded as stated in respect of the hold loading. However, in respect of Passenger Cabin Loading the senior cabin crew member usually confirms the number of passengers actually on board by means of a headcount after boarding has been completed.

Electronic Flight Bag generation of Load and Trim data

For some flights, especially but not only cargo flights, the flight crew have an electronic flight bag (EFB) which they use to calculate aircraft performance data, which takes account of the completed load and trim sheet. They also use the EFB to make the load and trim calculations themselves, so that once it has been checked, all that is required is that a copy be left with the agent at the point of departure. Clearly, it is vital that a rigorous process of crosschecking is included in the preparation of such documentation to avoid input errors. Crosschecking does not mean simply repeating the numbers selected/presented but also confirming that they make sense in relation to the actual situation.

Provisional and Final Load Sheets

DCS and the communication facility afforded by ACARS (Aircraft Communicaitons Addressing and Reporting System) has allowed aircraft commanders to be given substantially complete and correct loading documents with ‘provisional’ status in plenty of time before STD; ‘final’ status documents with highlighted minor amendments (also known as Last Minute Changes - LMC) can be generated as the aircraft leaves the gate for acceptance via ACARS at any time before take-off commences.

Adjustment of the Last Minute Changes (LMC)

It is often necessary to adjust the loadsheet after completion. These adjustments are called last minute changes (LMC). The LMC process is a way to enter late alterations/updates to a final manual or electronically produced loadsheet, without requiring revisions to the main body or the preparation of a new document. Guidance material on the LMC is made available by UK CAA: CAP 1008 Last minute changes (LMC).

Any LMC increase or change must not exceed the:

  • allowable underload calculation (Underload is the weight that still is available until the first limiting maximum weight is reached).
  • maximum mass and balance limits for zero fuel, take-off or landing
  • limitation of any compartment that is intended to be used

There is a maximum allowable change to the number of passengers or hold load as an LMC, which will be specified in the individual operator’s Operations Manual for each aircraft type. Operators must also specify a similar rule for changes to the balance condition, to be defined in index units. If there are changes to fuel quantities and/or locations, the weight and balance figures should be fully recalculated and new documentation produced because of the significance in terms of the aircraft mass and balance condition. However, some operators may permit fuel LMCs for lesser quantities, so fuel mass and index data must be made available and should be checked.

If any LMC occurs after the completion of the mass and balance documentation, it must be brought to the attention of the captain and clearly entered on the documentation. The captain should amend the mass and balance sheet, but it is essential that it is recorded on the copy kept at the point of departure.

Risks arising from aircraft loading

The primary risks arise from the aircraft being ‘set up’ for take off with incorrect pitch, trim and/or take off reference speeds. This can arise in one of three ways:

  • The aircraft is not loaded in the way stated on the accepted load and trim sheet (applicable to any load sheet type)
  • The aircraft load and trim sheet uses correct input data but the output data is wrong (applicable to manual load sheets)
  • The flight crew apply the (correct) load and trim data incorrectly when using it to calculate aircraft take-off performance data, including reference speeds and scheduled thrust settings.
  • The hold load is not properly secured or contains prohibited or incorrectly packed items.

Consequences of actual misloading or incorrect input of load-related data

Either actual miss-loading of an aircraft or incorrect use of correct load related data for aircraft systems set up can severely affect aircraft performance, stability and control. Loss of Control may occur during an attempted take off or during subsequent flight because either:

  • an attempt (usually inadvertent) is being made to operate the aircraft outside the AFM limits, or
  • flight crew actions to control the aircraft are ineffective because the aircraft is unable to achieve the expected performance, whether in relation to manually selected or FMS generated safety speeds on the ASI(e.g Vr) or selected engine thrust parameters.

One potential consequence of an error in loading or data entry is tailstrike on take off. This will usually lead to fuel dumping and a return to the take-off airfield, without pressurizing the cabin and is not career enhancing for any of the pilots, even the relief crew. Even more serious, Runway Excursion has been a regular result of errors of both these types in the past, whether or not an Rejected Take Off has been attempted. Given the potential severity of a mistake in loading, of transferring erroneous weight and balance figures however derived, of entering erroneous data into the aircraft management systems (FMS) or miss-setting ASI speed bugs, both pilots should always carry out Gross Error checks. Seniority does not imbue data entry infallibility! Amongst other checks, it is vital to confirm that the Zero Fuel Weight is sensible and then that the indicated Take-Off Weight is as expected.

For a more detailed discussion of the issues arising with hold and cabin loading, see Loading of Aircraft with Cargo and Passenger Cabin Loading which also have links to reports of investigations into specific outcomes consequent upon hold or cabin loading data being incorrectly calculated or applied.

Accidents and Incidents

The following events involved aircraft loading as a factor:

On 17 December 2017, it was discovered after completion of an Airbus A330-300 passenger flight from Sydney to Bejing that freight loading had not been correctly documented on the load and trim sheet presented to and accepted by the Captain and as a result, the aircraft had exceeded its certified MTOW on departure. The Investigation found that the overload finding had not been promptly reported or its safety significance appreciated, that the error had its origin in related verbal communications during loading and noted that the aircraft operator had since made a series of improvements to its freight loading procedures.

On 4 August 2018, a Junkers Ju-52 making a low level sightseeing flight through the Swiss Alps crashed killing all 20 occupants after control was lost when it stalled after encountering unexceptional windshear. The Investigation found that the pilots had created the conditions which led to the stall and then been unable to recover from it and concluded that the accident was a direct consequence of their risky behaviour. It found that such behaviour was common at the operator, that the operator was being managed without any regard to operational risk and that safety regulatory oversight had been systemically deficient.

On 29 April 2013, a Boeing 747-400 freighter departed controlled flight and impacted terrain shortly after taking off from Bagram and was destroyed by the impact and post crash fire and all occupants were killed. The Investigation found that a sudden and significant load shift had occurred soon after take off which damaged hydraulic systems Nos. 1 and 2 and the horizontal stabilizer drive mechanism components as well as moving the centre of gravity aft and out of the allowable flight envelope. The Load shift was attributed to the ineffective securing techniques employed.

On 2 July 2014, a Fokker 50 fully loaded - and probably overloaded - with a cargo of qat crashed into a building and was destroyed soon after its night departure from Nairobi after failing to climb due to a left engine malfunction which was evident well before V1. The Investigation attributed the accident to the failure of the crew to reject the takeoff after obvious malfunction of the left engine soon after they had set takeoff power which triggered a repeated level 3 Master Warning that required an automatic initiation of a rejected takeoff.

On 30 May 2019, a DHC8-200 departing from Nuuk could not be rotated at the calculated speed even using full aft back pressure and the takeoff was rejected with the aircraft coming to a stop with 50 metres of the 950 metre long dry runway remaining. The initial Investigation focus was on a potential airworthiness cause associated with the flight control system but it was eventually found that the actual weights of both passengers and cabin baggage exceeded standard weight assumptions with the excess also resulting in the aircraft centre of gravity being outside the range certified for safe flight.

On 16 April 2014, a pre-flight concern about whether a Boeing 777-200ER about to depart Singapore had been overfuelled was resolved by a manual check but an en-route fuel system alert led to close monitoring of the fuel system. When a divergent discrepancy between the two independent fuel remaining sources became apparent, an uneventful precautionary air turnback was made and overfuelling subsequently confirmed. The Investigation found that a system fault had caused overfuelling and that the manual check carried out to confirm the actual fuel load had failed to detect it because it had been not been performed correctly.

On 23 July 2015, an ATR72-600 crew suspected their aircraft was unduly tail heavy in flight. After the flight they found that all passenger baggage had been loaded in the aft hold whereas the loadsheet indicated that it was all in the forward hold. The Investigation found that the person responsible for hold loading as specified had failed do so and that this failure had not been detected by the supervising Dispatcher who had certified the loadsheet presented to the aircraft Captain. Similar loading errors, albeit all corrected prior to flight, were found by the Operator to be not uncommon.

On 20 February 2014, an ATR 72-600 crew mishandled their response to an intended airspeed adjustment whilst using VS mode during descent to Sydney and an upset involving opposite control inputs from the pilots caused an elevator disconnect. The senior cabin attendant sustained serious injury. After recovery of control, the flight was completed without further event. Post flight inspection did not discover damage to the aircraft which exceeded limit and ultimate loads on the stabilisers and the aircraft remained in service for a further five days until it was grounded for replacement of both horizontal and vertical stabilisers.

On 19 August 2013, a fire occurred in the right engine of a Douglas DC3-C on take off from Yellowknife. After engine shutdown, a right hand circuit was made in an attempt to land back on another runway but trees were struck and the aircraft crash-landed south of it. Emergency evacuation was successful. The Investigation found that a pre-existing cylinder fatigue crack had caused the engine failure/fire and that the propeller feathering pump had malfunctioned. It was found that an overweight take off had occurred and that various unsafe practices had persisted despite the regulatory approval of the Operator's SMS.

On 4 July 2009, an Airbus A332 being operated by Jetstar Airways on a scheduled passenger flight from Sydney to Melbourne carried a 750 kg ULD which had been expressly rejected by the aircraft commander during the loading operation without flight crew awareness. There was no reported effect on aircraft handling during the flight.

On 12 September 2003, a Saab 340B being operated by UK regional airline Loganair on a scheduled passenger flight from Aberdeen to Kirkwall experienced a loss of pitch control during landing at destination and the rear fuselage contacted the runway causing damage to the airframe. Once the aircraft had cleared the runway, some passengers and some of the hold baggage was removed before the aircraft was taxied to its parking position because of a suspicion that the aircraft might have been loaded contrary to the accepted load and trim sheet.

On 7 December 2003, a Boeing 737-800 being operated by SAS on a passenger charter flight from Salzburg, Austria to Stockholm Arlanda with an intermediate stop at Goteborg made a high speed rejected take off during the departure from Goteborg because of an un-commanded premature rotation. There were no injuries to any occupants and no damage to the aircraft which taxied back to the gate.

On 25 December 2003, a Boeing 727-200 being operated by UTA (Guinea) on a scheduled passenger flight from Cotonou to Beirut with a planned stopover at Kufra, Libya, failed to get properly airborne in day VMC from the 2400 metre departure runway and hit a small building 2.45 metres high situated on the extended centreline 118 metres beyond the end of the runway. The right main landing gear broke off and ripped off a part of the trailing edge flaps on the right wing. The airplane then banked slightly to the right and crashed onto the beach where it broke into several pieces and ended up in the sea where the depth of water varied between three and ten metres. Of the estimated 163 occupants, 141 were killed and the remainder seriously injured.

On 12 January 2003, a Boeing 737-800 being operated by Dutch airline Transavia on a passenger charter flight initially going from Rotterdam to Maastrict-Aachen was obliged to reject its take off on Runway 24 at Rotterdam after it pitched nose-up just after take-off thrust had been selected. The pitch up movement only stopped when the aft fuselage and the tailskid assembly contacted the runway and only when the flight crew rejected the take-off did the aircraft nose gear regain ground contact. The aircraft was damaged and unfit for flight but able to taxi back to the terminal to allow the uninjured passengers to disembark.

On 8 January 2003, a B190, operated by Air Midwest, crashed shortly after take off from Charlotte, NC, USA, following loss of pitch control during takeoff. The accident was attributed to incorrect rigging of the elevator control system compounded by the airplane being outside load and balance limitations.

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